A. Siemko and N. Catalan Lasheras Insulation vacuum and beam vacuum overpressure release – V. Parma Bus bar joints stability and protection – A. Verweij.

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Presentation transcript:

A. Siemko and N. Catalan Lasheras Insulation vacuum and beam vacuum overpressure release – V. Parma Bus bar joints stability and protection – A. Verweij Improved anchoring of SSS with vacuum barrier to avoid displacement – O. Capatina QPS Upgrade and Re-commissioning– R. Denz Risk Analysis for the Different Consolidation Proposals – J. Strait

V. Parma

 Insufficient pressure relief devices in the current cryostats  Vacuum vessel and vacuum barrier designed to keep internal pressure ≤ 1.5 bars, for a helium release with mass flow ≤ 2 kg/s  Pressure estimated to 7 bars on September 19 th. Peak mass flow 20kg/s.  MCI could create a helium mass flow of 40kg/s MCI ?

 Use all existing ports as pressure relief ports  BPM, vacuum and cryo-instrumentation ports in the SSS  x10 cross section  Maximum pressure reduced to about 3 bars  Vacuum barrier and cold posts still designed for 1.5 bars but may resist 3 bars  Critical now the floor and jack fixations  Pressure relief spring tested  Can be implemented in cold sectors

 Adding new DN200 relief devices in dipoles  x33 cross section  Maximum pressure below 1.5 bars. All other systems are now conform  Special cases in the mid-arc and DS  Studied and feasible  Can only be implemented in warm sectors  Implementation end of week 14 for four warm sectors

 Testing vacuum barriers and cold posts  Stand-alone magnets and inner triplets  Beam insulation vacuum From the discussion  DFBs  Derogations from safety in case of partial solution

O. Capatina

 Failure of some supports of SSS in sector 3-4 due to longitudinal loads on September 19 th.  If internal pressure above 1.5 bars, support system is insufficient.  Nominal operation for supporting system 0.1MPa, exceptionally 0.15MPa (80kN, exceptionally 120kN)  Failure limit 150kN  Coherent system  vacuum barrier/cold post/jacks/floor  New requirements 240kN

 Anchoring of the jacks  Tested in the tunnel floor(SX4) up to 380kN  Drilling authorised without liquid helium  Installation ok with liquid helium  2 weeks per sector plus alignment. Total of 25 days.  CHF for all 8 sectors.

Basically the same as in previous presentation  DFB’s stand alones, inner triplet  Testing of the vacuum barrier and cold post From the discussion  Do we need this if DN200 is implemented in all magnets? 1.5 bars could be marginal for the current solution

A. Verweij

 An interconnection opened on September 19 th.  Probably a bad splice. Two potential scenarios  Bad electrical and thermal contact  Between joint, u-shape and wedge  Between u-shape and wedge and bus-bar (longitudinally)  Resistive cable plus longitudinal discontinuity

 Fast localised thermal runaway  Stable resistive heating below 7.5kA. Slow voltage increase much below QPS threshold (mV)  Fast normal zone development  Temperature increases rapidly above melting point

 QPS threshold of 0.3 mV. Integration time 10s  Detects any resistance larger than 25 nOhms up to nominal current  Avoid bad splices  Excessive longitudinal gap, Lack of solder  Clamping

 QPS system cannot protect the circuit in case of a sudden mechanical opening of the joint  Other bus-bar types (6 kA, pigtails...) From the discussion  Operability  Clamping

R. Denz

 Symmetric quenches between apertures went unnoticed for more than half a second  Local bus-bar protection capable of detecting bad splices  Threshold 0.3mV, integration time 10s

 Detection of symmetric quenches:  Compare consecutive magnets  New card design  Not in the baseline for 2009 before Chamonix mtg. (E<5TeV)  Splice detection  Uses existing voltage taps in the diode  Uses protection cards for HTS leads  Regular scans during operation  Both solutions require additional cabling (240Km)

 Radiation hardness of the electronics  Verifying the cabling  Commissioning of the new system  In the critical path From the discussion  Beam induced symmetric quenches  Spurious triggers

J. Strait

 Improved QPS system for detection of bad splices in bus-bars  Added procedures  Calorimetric measurements  Snapshot on individual magnets  Snapshot in bus-bars  Avoid collateral damage  Additional DN200 ports in dipoles in half of the machine  Additional pressure relief ports in SSS in all LHC  Improved anchoring for SSS with vacuum barrier

 Pressure relief in vacuum system  Improve pressure relief in DFBs, stand alone magnets and inner triplet  Anchoring of the DFBA supports  Intelligent reaction to quenches in bus-bars and other sensible equipment  opening of the quench release valves at a lower pressure  Firing more quench heaters to speed up current decay

 Add DN200 ports in all dipoles in the machine (warm-up other 4 sectors)  Not recommended if prevents running this year  Add burst disks in the vacuum system  Recommended at least for warm sectors  Adding DN200 in DFB  Recommended at least for warm sectors  Intelligent reaction to quenches  Should be studied carefully  not mandatory

 What if additional bad splices in the magnets are found?  When machine is cold  Other mitigation measures will minimize the risk of an accident  Limited damage to one or two dipoles  Leave it and change it in the next shutdown  By analysis of the already taken data (snapshots and cold tests)  Change the magnet as soon as possible

 What if additional splices are found in the bus- bars?  It will be detected when cold  Warm up and repair the splices  What energy should we run in TeV is achievable, safe AND useful

 The incident in sector 34 revealed needs of enhanced:  Early spotting of possible origins of faults  Enhanced prevention of initial faults  Mitigation of consequences  Means were developed and implementation scenarios proposed to a happy landing wherever we're falling to with the electrical splices of magnet circuits Thanks to all speakers