LHQ Coil Fabrication Experience and Plan Miao Yu 04/08/2013.

Slides:



Advertisements
Similar presentations
HQ & LHQ End Parts Miao Yu Fermilab 08/27/12. HQ parts All the spacers are arriving within a week. 2.
Advertisements

LQ Reaction & Impregnation Tooling Internal Review F. Nobrega, N. Andreev August 13, 2007.
Long HQ coil drawings now available 1 Miao Yu. Dead voltage taps in TQ/LQ/HQ coils Inner layer: 24, outer layer: 12 (33 inner/23 outer per coil for TQ/LQ/HQ)
LHQ Coil 02 Winding and Curing Plan Miao Yu 03/21/13.
LHQ Coil 1 OL Curing LHQ Coil 1 Shipping Miao Yu 02/28/2013.
SQXF Practice Winding 1 L2 winding Miao Yu 01/23/2014.
EuCARD-HFM ESAC review of the high field dipole design, 20/01/2011, Maria Durante, 1/40 EuCARD-HFM ESAC Review of the high field dipole design Fabrication.
Racetrack Coil Technology – G. Ambrosio 1 LARP DOE review – FNAL, June. 5-6, 2007 BNL - FNAL - LBNL - SLAC Racetrack Coil Technology (LR, SQ) & other Supporting.
Dan Cheng H. Felice, R. Hafalia QXF Structures Video Meeting July 10, 2014 Coil Handling for Magnet Assembly Status Update.
Preliminary Design of Nb 3 Sn Quadrupoles for FCC-hh M. Karppinen CERN TE-MSC.
Design and Plans for Introducing Flexible End Parts Steve Krave 15 October 2013.
SQXF 25 m Cable Practice Winding at LBNL Miao Yu Dan Cheng 10/31/2013.
LHQ Coil Fabrication Experience and Plan Miao Yu 04/08/2013.
Nb3Sn Cable and Insulation for LARP High-Gradient Quadrupole Magnets
Coil Design and Fabrication Miao Yu Outline Introduction Coil Design –Coil Pole –Coil End Parts –Coil Insulation Coil Fabrication –Winding.
HQ Coil 23 and 25 Status LARP Video Meeting September 19, 2013 Dan Cheng.
E. Cavanna, N. Bourcey, P. Ferracin, S. Izquierdo Bermudez, J. Mazet, J. C. Perez, Francois-Olivier Pincot, X. Sarasola
Coil parts & Instrumentation issues for LQ/HQ coils tested at Fermilab HQ/LHQ coil parts task force.
Fred Nobrega. 9 Dec 2014 Model Design & Fabrication – FNAL Fred Nobrega 2 Outline Background Mechanical Design Model Magnet Features Coil Technology and.
F. Borgnolutti November 14 th nd HiLumi Collaboration Meeting Frascati HQ coils: History & Performance.
Ultra-Compact Electrical Machines for Wind Energy DE-FOA : Demo Machine C. L. Goodzeit and M. J. Ball May 1, 2014 Part 1: Design and Construction.
Susana Izquierdo Bermudez. SLS parts 2 Our support is in the nose area that the reason we got the deviations in this area. For the next parts we do the.
FNAL QXF Curing Mold Miao Yu, FNAL 05/07/2013. FNAL Short Curing Press 2 2 meter long Capacity (pump psi) Max. force/cylinder kN (ton) Spacing cm(inch)
E. Cavanna, N. Bourcey, P. Ferracin, S. Izquierdo Bermudez, J. Mazet, J. C. Perez, F.O. Pincot, X. Sarasola
DOE Review of LARP – February 17-18, 2014 Coil Design and Fabrication Miao Yu February 17,
11 T Dipole Experience M. Karppinen CERN TE-MSC On behalf of CERN-FNAL project teams The HiLumi LHC Design Study (a sub-system of HL-LHC) is co-funded.
LHQ Coil 02 Winding and Curing Miao Yu 07/11/2013.
Fred Nobrega, Nikolai Andreev 21 September, 2015.
Coil Parts Task Force Video MtgG. Ambrosio 11 HQ/LHQ Coil Parts Task Force January 6, 2012 BNL - FNAL - LBNL - SLAC.
S. Caspi, LBNL HQ Progress and Schedule Shlomo Caspi LBNL LARP Collaboration Meeting – CM13 Port Jefferson November 4-6, 2009.
Helene Felice 11/16/2011 LARP Collaboration Meeting 17 1 st HiLumi Collaboration Meeting CERN Status on HQ Coil Design and Fabrication.
D. Smekens. 2 Coil ID  CableCu DUMMY Cu DUMMY WST DUMMY RRP 54/61 DUMMY RRP 108/127 RRP 108/127 RRP 108/127 RRP 132/169.
1 Quench Protection Workshop - 04/29/2014 QXF heater design M. Marchevsky, D.W. Cheng (LBNL) E. Todesco (CERN) T. Salmi (Tampere UT) G. Chalchidze, G.
Helene Felice HQ Test Results Review Thursday December 16 th Overview of HQ coils and Magnet.
FRESCA2 Technical Meeting 5-Validation of coil winding with Cu coils Françoise Rondeaux 09/06/ CEA-Irfu-SACM-LEAS - 5-Rondeaux- FRESCA2 Technical.
LARP Collaboration Meeting Racetrack Coil Fabrication
Dan Cheng, Helene Felice 4/8/2015 MQXFS-D Build-up LBNL “Lessons Learned”
MQXFS Coil V1 Fabrication Status -Winding and Curing Miao Yu
LHQ Coil 03 Winding and Curing Miao Yu, Steven Krave 05/23/2014.
QXF Coil Fabrication: Baseline Decisions QXF Coil Working Group Video Meeting (Revised from discussion during presentation) Dan Cheng April 16, 2013.
L/R Coil Asymmetry Coil Fabrication Working Group Trey Holik Wednesday, June 3 rd 2015.
SEPT 20, 2006 T. Brown, M. Cole, P. Fogarty, P. Goranson, K. Freudenberg, D. Williamson NCSX STAGE 2 COIL TO COIL ASSY.
1 FPA Stage 2 MC Flange Assembly Issues and Design Proposals June 20, 2006 T. Brown.
Fabrication of test coil for D1 2m model Michinaka SUGANO KEK WP3 meeting 08/10/2014.
SQXF Cu Cable Winding Test at LBNL Dan Cheng Dec 17, 2013.
QXF Coil Insulation during Each Step QXF Coil WG Miao Yu 08/22/2013.
DOE Review of LARP – February 17-18, 2014 SQXF Coil Design and Fabrication Winding and Curing Miao Yu February 17,
Cold Mass and Assembly Tooling Design, Procurement Status and Assembly Plan Igor Novitski Fermilab 15 T Dipole Design Review April 2016 April 28-29,
CERN MBHSM0101 and Plan for Future Models F. Savary on behalf of the 11T Dipole Project Team.
LARP DOE Review, 7/9/2012Long Quadrupole – G. Ambrosio 1 Long Quadrupole Program Giorgio Ambrosio DOE Review of the LARP Program SLAC July 9-10, 2011 LQ.
QXF Reaction / Impregnation Fixtures J. Schmalzle 4/9/13.
QXF Winding/Curing Tooling and Curing Mold Miao Yu, FNAL 04/09/2013 CM20_Napa Valley, CA.
Dan Cheng 8/27/2015 MQXFS1 Observations and Feedback from the Assembly Processes, Part II.
LHQ Coil Design and Features Miao Yu Fermilab May 09, 2012.
2 nd LARP / HiLumi Collaboration Mtg, May 9, 2012LHQ Goals and Status – G. Ambrosio 11 LHQ Goals and Status Giorgio Ambrosio Fermilab 2 nd LARP / HiLumi.
Pocket and Metric Hole in End Parts Miao Yu 02/25/2014.
1 Long QXF Mirror Fabrication (MQXFPM1) Rodger Bossert HiLumi-LARP Collaboration Meeting May 18-20, 2016 SLAC R. Bossert - HiLumi Collaboration Meeting.
LHQ01 IL Curing Miao Yu 01/31/2013. LHQ IL Packing for Curing 2.
Page 1 TQC Mechanical Model Igor Novitski / Rodger Bossert May 24, 2006 Results of MM#4 and MM#5.
QXF Coil Fabrication & Tooling Reaction / Impregnation
Procurement Status Miao Yu 11/19/2013.
Coil Design and Fabrication
Model magnet test results at FNAL
Winding tests on Roebel cables
HQ Coil 19 Test Impregnation
11 T dipole coil features and dimensions
Mechanical stability and QXF coil winding
MQXF updates P. Ferracin October 9th, 2014.
MQXF coil cross-section status
Coil Fabrication Status
Presentation transcript:

LHQ Coil Fabrication Experience and Plan Miao Yu 04/08/2013

Introduction LHQ is 3.3 m version HQ coil Check fabrication technology for the scaling up. Totally 3 coils will be fabricated, and one coil will be tested in the mirror structure Winding and curing at FNAL; reaction and impregnation at BNL LHQ coil 01 is the first coil (practice coil), to verify the fabrication procedure and all the tooling Current status: LHQ coil 01 is being reacted at BNL, this talk is focusing on winding and curing. CM20_Napa Valley, CA 2

Outline LHQ Coil 01 fabrication experience –Cable during winding –Coil parts during winding and curing –Curing: binder, pressure and coil size –Other discrepancy report –Lifting fixture LHQ Coil 02 Plan CM20_Napa Valley, CA 3

Cable during winding 360 ° twist was applied Winding tool was used for both IL and OL First turn in IL and OL, the tension was 20 lbs (9 kg) IL tension 30 lbs (13.6 kg), OL 35 lbs (15.9 kg) Location # of pop strands FixedNote IL LE 3 rd 1By hand IL LE 6 th 1 Paint binder and cured IL RE 6 th 2By hand RE spacer was not aligned, cable was back wound, causing pop strands IL RE 8 th 1By hand IL RE 11 th 2By hand The winding mandrel was rotate too fast IL RE 14 th 4 Paint binder and cured The winding mandrel was rotate too fast OL LE 2 nd 1 Paint binder and cured L1-L2 cable jump section, bend during L1 curing preparation OL RE 6 th 1 Paint binder and cured OL LE 11 th 1 Paint binder and cured Might be avoided CM20_Napa Valley, CA 4

Coil Parts: Wedge Insulation The sleeve was cut about the length of the wedge before gluing, causing the insulation loose at the end. (Solu: cut longer length insulation or glue the end first and then cut the insulation) Two ways used to glue the insulation to the wedge: 1.Paint binder along the wedge and cure in the oven at 150°C for 1.5h X (debond, fluffy) 2.Paint binder only at the ends and cure using heat gun ˅ CM20_Napa Valley, CA 5

Coil Parts: Plasma Coating To increase the dielectric strength coil to parts & coil to ground Although the coating is porous, it will be filled with epoxy to gain better dielectric strength. LHQ coil end parts were modified from the latest HQ design –7 mil was removed from the surface where the insulation is inserted. –Besides, 10 mil was removed from the surface where plasma coating is applied (in red). Coating thickness did not meet the spec. from both vendors. Specs: 9mil±1mil (225µm±25µm) for flat surface; 8mil±2mil (200 µm±50µm) for the rest of surfaces The coating surface is more abrasive than the metal surface. It may damage the insulation and the cable without any indication, so be very careful when install the parts. Coating chips off when opening the slit 5 mil (125µm) coating thickness CM20_Napa Valley, CA 6

Coil Parts: End Parts Fitting IL and OL saddles do not fit due to coil ends jumping up (new hold-down tooling was designed and practiced at LBNL) After curing, the IL saddles were pushed in easily and fit pretty well, and OL still do not fit due to other issue (binder). 1 mil Mica was added at the tip of the parts to have better slipping plane. During winding After curing CM20_Napa Valley, CA 7

Curing: Binder 120 g binder was applied to the IL, and 140 g was applied to the OL Scale up from HQ coil 1.IL 142 g (44 g for HQ) 2.OL 209 g (65.4 g for HQ) Too much binder applied to the interlayer insulation (saturated before curing, very rigid after curing) HQ: mm, LHQ: mm HQ: mm, LHQ: mm Cable separation Wedge jumping up Saddle not fit CM20_Napa Valley, CA 8 Outer Layer Layers separation

Curing: Pressure Inner layer curingLoad 1Load 2Load 3 Mandrel cylinder45 kN/m68 kN/m90 kN/m Platen cylinder450 kN/m670 kN/m890 kN/m Room T gap (mm) °C gap (mm) °C gap (mm) MPa 30 MPa Max. load/cylinder (ton/kN) Spacing (inch/cm) Max. load/unit Length (kN/m) Max. load for LHQ (kN/m) Main Cylinders200/178012/305934~1780 Mandrel Cylinders15/1346/15894~180 Outer layer curingLoad 1Load 2Load 3Load 4Load 5 Mandrel cylinder45 kN/m68 kN/m90 kN/m135 kN/m180 kN/m Platen cylinder450 kN/m670 kN/m890 kN/m1335 kN/m1780 kN/m Room T gap (mm) °C gap (mm) °C gap (mm)----0 CM20_Napa Valley, CA 9

Curing: Coil Size In LHQ coil 01 during curing, the coil was over compressed by ~125 µm azimuthally to its nominal size. However, this additional 125 µm shim was applied from saddle to saddle extension, and these end parts are in nominal size CM20_Napa Valley, CA 10 Midplane shim LHQ coil nominal size azimuthally: 125 µm to the midplane (the gap is for ground insulatoin)

Other DR Coil Parts: Coating chips off around slit area, causing by the vendor Coil Parts: IL LE saddle and splice block did not align properly after coating, and was fixed (should be done before coating). Coil Parts: ¼" key stock was used instead of ¼" dowel pin due to undersize pin hole. Instrumentation: Voltage tap A3 and B8 were broken. The thickness of VT is thinner than nominal 1.5 mil (38 µm). CM20_Napa Valley, CA 11

Lifting Fixture Need one more clamp to hold down the coil RE CM20_Napa Valley, CA 12

LHQ Coil 02 Plan  Tooling Preparation and Modification  Coil parts Open the pin holes on the pole using ” reamers.(6.35 mm dowel pin, mm hole, which can be adopted by QXF design +13µm/-0) Add slit to the saddles (after HQ practice coil) Plasma coating all parts Winding and curing the coil without splice block (for LQXF)  Pole Gap and wedge gap Pole gap will be determined after LHQ 01 reaction Wedge gap will be increased (scale up from HQ wedge gap)  Cable Try no twist on the cable between spool and the coil Use winding tool and hold down tooling at the coil end Use binder when pop strand is hard to fix by hand Winding tension: 20 lbs for the first turn, and then 35 lbs CM20_Napa Valley, CA 13

LHQ Coil 02 Plan cont.  Binder Use less binder on interlayer insulation and quantify the amount Use the proper amount of binder for L1 and L2 (scale up from HQ coil)  Others Try to fit the end parts without 1 mil mica Over compress the coil straight section by 5 mil Use 10 mil Mylar as curing radial shims instead of SS Need more 1.5 mil (~38 µm) thick voltage tap Add one more clamp to the lifting fixture to secure the RE  Schedule  Coil parts will be plasma coated in end of April.  After LHQ coil 01 reaction, start fabrication of LHQ coil 02 around early May. CM20_Napa Valley, CA 14