Frequency analysis of quad noise prototype Justin Greenhalgh summarising work of Tim Hayler and others in T060059-00-K LSC Meeting, LHO, March 2006 LIGO-G060107-00-K.

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Presentation transcript:

Frequency analysis of quad noise prototype Justin Greenhalgh summarising work of Tim Hayler and others in T K LSC Meeting, LHO, March 2006 LIGO-G K

LIGO-G K 2 Simple bolted structure Screws

LIGO-G K 3 Simple bolted structure FastenersContact surface stiffnessFastener modulus Hz bondedProgram controlledNA424 "0.01" 402 "0.001" 328 Boltssuppressed2E11 Pa 224 ""2E15Pa 356 Screwssuppressed2E11 Pa298 ""2E15Pa 350 Boltsfrictionless2E15Pa 405 screws"2E15Pa 408

LIGO-G K 4 Simple bolted structure – conclusions Plenty of opportunity to vary the result with different representation of bolts/screws etc.

LIGO-G K 5 Asymmetric structure Idea: outriggers on one side are at a better angle Downside is that the outriggers at the other side are ineffective – not clear if the benefits will outweigh the disadvantages Result – did not improve things 53Hz 52.5Hz

LIGO-G K 6 Change thickness of top plate Extra stiffness and extra mass – did not help

LIGO-G K 7 Modify bracing arrangement and reduce mass of implementation ring Reduce from three rings of bolts to one ring of bolts at implementation ring But bolts not in the model, so not surprising this did not help the results Modify bracing (outriggers) by looking at load paths and trying to straighten them Probably we did not put enough mass into the outriggers – but even so it’s a surprise that it did not help at all Bottom line result: Before = 77.8 Hz After = 77.8 Hz

LIGO-G K 8 Modify bracing arrangement and reduce mass of implementation ring

LIGO-G K 9 Varying the clamping method on the top plate case one. Fixed supports are maintained on the outriggers assembly pads to the implementation ring (implementation ring not included in model) and around the perimeter of the top plate. case two. Fixed supports are maintained on the outriggers assembly pads to the implementation ring (implementation ring not included in the model) and on the entire surface of the top plate.

LIGO-G K 10 Varying the clamping method on the top plate CaseTop plate joined to face plates by contactFrequency Hz One Bonded Onescrewsfrictionless onescrewsnone107 * twoscrewsfrictionless onescrews1mm gap106.8 * twoscrews1mm gap

LIGO-G K 11 Varying the clamping method on the top plate Conclusions: Varying the style of clamping of the top plate does not make much difference So the plate is not “panting” to a significant effect Varying the style of the bolting model does not make much difference either Disappointing because these were obvious candidates for improving things

LIGO-G K 12 Analysis of differences in CIT tests Typical CIT test configuration

LIGO-G K 13 Analysis of differences in CIT tests Calum’s clean room results Hz ∆ FEA results Hz ∆ Implementation ring, Top plate and outriggers Top plate no outriggers Top plate no outriggers and no plates on the side Top Plate and one half of the structure.1722

LIGO-G K 14 Analysis of differences in CIT tests Conclusion: The side plates don’t change things nearly as much in the real world as the FEA suggests – so maybe it’s the way THEY are bolted that we should look at.

LIGO-G K 15 “X-brace” idea to make the outriggers work harder

LIGO-G K 16 “X-brace” Theory: Create “hard points” at the tops of the X-braces. X-braces extend the “triangles” idea used successfully in the top structure Result: No change in frequency Maybe because the X-braces are not meaty enough compared to the side plates they are trying to stiffen

LIGO-G K 17 Struts Break the envelope But give good results 50od 40id ~1.8m long 35 degrees to vertical

LIGO-G K 18 Struts modeFrequency Hz Comment 1 st 75 Internal mode in brace 2 nd 78 “ 3 rd 80 “ 4 th 80 “ 5 th 85 Lateral mode not improved by brace 6 th 129 THIS IS THE ONE

LIGO-G K 19 Struts modeFrequency Hz 1 st 85 2 nd 129 Was ~77 Hz 3 rd th th th 227 Use braces with no density to remove internal modes:

LIGO-G K 20 Removal of central side-plates SIMPLE experiment, simply suppressed some parts of the structure Improved primary beam modes by ~10 Hz Modes were 77 & 86 Hz Became 87 & 94 hz

LIGO-G K 21 Removal of central side-plates 77 Hz 87 Hz

LIGO-G K 22 Conclusions so far Modelling bolts has the potential to build a model that matches the tests with a credible rationale And hence making things better by use of modified bolted joints eg in compression/tension rather than shear. Making the structure asymmetric did not help Initial ideas did not help Modify thickness of top plate, minor mods to outriggers Reducing number of bolted joints in implementation ring may help Need to figure out how to model bolted joints to assess this Changes to clamping of top plate and modified bolting between side plates and top plate did not help More radical change to outriggers (X-braces) did not help But we think they will help if we trade mass into them Struts outside the envelope helped a lot But introduce internal modes of their own that would need fixing This should only be a fallback Removing the central plates helped ~10Hz But introduces issues with assembly and potentially a big issue with welding

LIGO-G K 23 Options for the structure Improve performance of structure Tweaks to make better use of mass Understand and then fix bolted joints Strut to improve stiffness Damping in control system Electronic Mechanical (strut or tuned-mass) If we introduce a strut would we rather have better stiffness or better damping? (cannot do both) And what about parasitic modes that come with the strut?