Oncor Electric Delivery Company LLC TOGETHER WE DELIVER ODESSA UPDATE Jan 22, 2013 Presentation to ERCOT Regional Planning Group Austin, TX Mike Juricek.

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Presentation transcript:

Oncor Electric Delivery Company LLC TOGETHER WE DELIVER ODESSA UPDATE Jan 22, 2013 Presentation to ERCOT Regional Planning Group Austin, TX Mike Juricek Senior Manager

1 Mike Juricek - ERCOT RPG Meeting01/18/2013 WEST TEXAS

2 Mike Juricek - ERCOT RPG Meeting01/18/2013 ACTIONS & IMPROVEMENTS (Completed & Underway) 2011 Rebuild Holt South – Goldsmith 69 kV Line as Double-Circuit 138 & 69 kV Line and Convert Goldsmith to 138 kV Jun Inspected Odessa North 138/69 kV Autotransformer and Critical Contingency Lines Aug 2012 Installed Online Temperature Monitoring and Auxiliary Oil Cooling on the Odessa North 138/69 kV Autotransformer Rating to 99 MVA (Nameplate 75 MVA) Sep 2012 Implemented Changes in System Configuration to Limit Flow through the Odessa North Autotransformer Sep 2012 Upgraded Terminal Equipment on Moss – Westover 138 kV Line Sep 2012 Upgraded Terminal Equipment Odessa North – Holt 69 kV Line Sep 2012 Upgraded Terminal Equipment Odessa North – Cowden North 69 kV Line Sep 2012 Increased Emergency Rating of Switches at Judkins on Permian Basin – Odessa EHV 138 kV Line Sep 2012 Convert Goldsmith Gulf to 138 kV (Approx 6 MW of load when converted) Oct 2012 Replace Odessa North 138 kV/69 kV Autotransformer with 100 MVA Nameplate (Rated 125 MVA Emergency) Nov 2012 Increase rating (operating temp) of Moss – Holt 138 kV Line Dec 2012 (Operating temperature cannot be increased until four customer-owned distribution feeder crossings are lowered which cannot be completed in 2012) Increase rating (operating temp) of Moss – Odessa EHV 138 kV Line Dec 2012

3 Mike Juricek - ERCOT RPG Meeting01/18/2013 LONGER TERM CONGESTION RELIEF PROJECTS 2013 Increase rating (operating temp) of Moss – Holt 138 kV Line to 100°C (897 A. to 990 A.) May 2013 Create New 138 kV circuit from Moss to Goldsmith Junction to Holt by: Rebuilding Goldsmith – Goldsmith South 69 kV Line as Double-Circuit 138 & 69 kV Line and Converting Goldsmith South to 138 kV Approx 31 MW Mar 2013 Complete Holt – Goldsmith 138 kV Connection May 2013 Rebuilding Goldsmith South – Goldsmith Junction 69 kV Line as a Double-Circuit 138 & 69 kV Line Jun 2013 Connecting Goldsmith Junction to Moss – Ector County North 138 kV Line Jun 2013 Reconductor Odessa – Odessa North 138 kV Line with ACCC Conductor Dec 2013 Reconductor Moss – Holt 138 kV Line with ACSS/TW Conductor Dec Add 345 kV Breakers at Moss Switching Station May 2014 Establish Odessa North 138 kV Switching Station May 2014 Rebuild Odessa North – Goldsmith Junction 69 kV Line as a Double-Circuit 138 & 69 kV Line May 2014 (disconnect from Moss – Ector County North 138 kV Line) Upgrade Moss – Westover 138 kV Line May 2014 Upgrade Odessa EHV – Big 3 Tap – Odessa Southwest – Moss 138 kV Line Dec 2014

4 Mike Juricek - ERCOT RPG Meeting01/18/2013 LONGER TERM CONGESTION RELIEF PROJECTS 2015 Construct Permian Basin – Culberson 138 kV Line (RPG Review & CCN Required) May 2015 Construct Moss – Permian Basin Double-Circuit 345 kV Line (RPG Review & CCN Required) May 2015 Construct Odessa EHV – Moss (connect to one Permian Basin circuit) 345 kV Circuit on Existing Structures May 2015 Add Additional 345 kV Breakers at Moss Switching Station to support new circuit to Permian Basin May 2015 Establish 345 kV Switching Station and Install 600 MVA 345/138 kV Autotransformer at Permian Basin May 2015 Under Consideration Upgrades to Address Issues in North Andrews and Odessa North Areas New 345/138 kV Station North of Midland, East of Holt Dynamic Reactive Device Andrews/Holt Area (dynamic studies needed) New 345/138 kV Station South of Midland Odessa

5 Mike Juricek - ERCOT RPG Meeting01/18/ Construction

6 Mike Juricek - ERCOT RPG Meeting01/18/ Construction

7 Mike Juricek - ERCOT RPG Meeting01/18/ Construction