ESLS-RF Meeting 2004 Status of the HOM Damped Cavity Project E. Weihreter / BESSY Project funded by the EC under contract HPRI-CT-1999-50011 for the HOM.

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Presentation transcript:

ESLS-RF Meeting 2004 Status of the HOM Damped Cavity Project E. Weihreter / BESSY Project funded by the EC under contract HPRI-CT for the HOM Damped Cavity Collaboration BESSY, Daresbury Lab, DELTA, MaxLab, NTHU Cavity concept and design goals Simulations and impedance measurement results Prototype cavity conditioning and first beam tests What lessons have we learned so far? Further developments Summary and outlook

ESLS-RF Meeting 2004 Fundamental mode frequency f = 500 MHz Insertion length L 0.7 m Shunt impedance R 4 M Max. thermal power P = 100 kW Compact design to fit into existing SR source tunnels Cavity Concept Design Goals

ESLS-RF Meeting 2004 Simulation Models S11=1 ~ 10 6 mesh points 2-3 days cpu time ~18* 10 6 mesh points 6-7 weeks cpu time

ESLS-RF Meeting 2004 Simulations and Impedance Measurement Results Tapered CWCT Homogenious waveguide with S11 = 1 boundary

ESLS-RF Meeting 2004 Threshold impedances for different rings

ESLS-RF Meeting 2004 Tuning and Cavity Test at ZANON S.p.A. / Italy

ESLS-RF Meeting 2004 Measured Impedance Spectra of

ESLS-RF Meeting 2004 Measured Cavity Parameters Parameter3D MWS Simulation Standard/New Method Measurement f0 (MHz) Q / Reff/Q0 (Ω) Reff (MΩ)3.73 / Nominal Frequency499.65MHz Tuning Range2MHz Shunt Impedance3.1MΩ Unloaded Q26692 Thermal Power Capability100kW Longitudinal HOM Impedance 4.8kΩ Transverse HOM Impedance 180kΩ/m Waveguide cut-off615MHz Coupling Range0-8 Insertion Length50cm Beam Hole Diameter TE11 cut-off TM01 cut-off mm GHz Resonant frequency vs. plunger position as measured and calculated.

ESLS-RF Meeting 2004 Prototype Cavity Conditioning Peak and average cavity input power during RF conditioning (p vac < 5*10 -7 mb) Vacuum conditioning procedure Increase in vacuum pressure around 200W and 600 W, however no serious multipacting thresholds observed

ESLS-RF Meeting 2004 Cavity installed in the DELTA Ring

ESLS-RF Meeting 2004 First Beam Observations at 1480 MeV DORIS Cavity HOM Damped Cavity CBM 55 is not driven by the cavity !!

ESLS-RF Meeting 2004 DORIS Cavity beam spectrum at low energy Final beam tests: measurement of coupled bunch instability thresholds at 540 MeV

ESLS-RF Meeting 2004 What lessons have we learned so far ? The tapered waveguides are the most critical components of the cavity about 60% of total manufacturing costs small tolerances vacuum brazing is a subtle technique, to be avoided where possible Engineering layout of e-beam welds and quality control during manufacturing must be improved Gaps between the ridges and the waveguide port wall should not be longer than 80 mm to avoid resonances coupling to the fundamental mode A CF 63 flange should be added at the end of the tapered waveguide Homogenous damping waveguides allow further reduction of HOM impedances

ESLS-RF Meeting 2004 Avoid long gaps coupling to fundamental mode gap

ESLS-RF Meeting 2004 Further Development: Homogenious ferrite loaded waveguide

ESLS-RF Meeting 2004 TDR measurement set-up CWCT used as adapter Ferrite load Circular ridged waveguide Low power model of a homogenous ridged waveguide load

ESLS-RF Meeting 2004 Summary A HOM damped prototype cavity has been built and tested under low and high power conditions Impedance measurements show that longitudinal HOM impedances < 4.8 k transverse HOM impedances < 180 k/m fundamental mode impedance 3.1 M Measurements are in good agreement with calculations: Simulation tools are reliable Successful high power operation up to 30 kW thermal power, no serious multipacting thresholds found Technical improvements modifications e-beam welds, avoid vacuum brazing where possible reduced gaps between ridges and CWCT port CF 63 flange at the end of the CWCT Conceptual and technical layout has been verified. Cavity design is ready for use. Outlook Final beam test of the cavity in DELTA at 540 MeV early in 2005 Development of a high power prototype for a homogenious wavegude load is under way to reduce manufacturing cost and further reduce HOM impedances by a factor 3-4