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A.Nichols CLRC1 SCT TE Close-Out Barrel TE, general observations (AN’s opinion only!) l Overall it was a success and all concerned worked extremely well.

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Presentation on theme: "A.Nichols CLRC1 SCT TE Close-Out Barrel TE, general observations (AN’s opinion only!) l Overall it was a success and all concerned worked extremely well."— Presentation transcript:

1 A.Nichols CLRC1 SCT TE Close-Out Barrel TE, general observations (AN’s opinion only!) l Overall it was a success and all concerned worked extremely well. There were many difficulties, but the TE was delivered on time l We had too much time: the basic design parameters were understood well enough to start work in 1995, but we spent too much time ‘refining’ our specification and the priority for detail design got muddled. Ironically, a shorter time scale might have helped as it would have compelled us to fix our ideas earlier l The End cap and barrel projects should have had a more common approach in terms of concept and manufacturing detail l Cost estimates were WILDLY optimistic by a factor of at least four

2 A.Nichols CLRC2 SCT TE Close-Out l We did not adapt very well to the many changes to the G&S specification and as a result we have a compromise »We missed the opportunity to use copper foil for shielding (as per the EC and TRT). If we had done this, improvisation as we progressed could have been made by robust soldered joints »Instead we have an all aluminium low-mass configuration –It worked fine and used robust bolted and gasketed joints, with minor connections by conductive adhesive –However, aluminium construction is not easy to improvise and I would not recommend it for the future l It’s inevitable that something like G&S is not well understood from the beginning and that it will evolve until the last minute, BUT we need to be better at managing the changes »Make sure you have a flexible design that can be changed easily as you go along or know what you are doing from the beginning

3 A.Nichols CLRC3 SCT TE Close-Out l Working with Lola Composites was a very positive experience. They should be encouraged for future projects »They worked in a very open way and were co-operative with problem-solving and liaison »They were three months late with delivery (this used our contingency and resulted in ‘just in time’ delivery, but this was understood from an early stage by both us and Lola: –Non availability of preferred pre-preg, derogation for new pre-preg with TIS –Breakage of OTE mould tool –Difficulties with co-curing the ITE and its shield »They provided us with false metrology data for the flawed MK2 ITE. However they rectified it very quickly at their expense – embarrassing though!

4 A.Nichols CLRC4 SCT TE Close-Out l The tender exercises were rather tedious »The first exercise was fruitless; the second yielded only two serious offers from 11? approaches »Luckily we made the right choice »The unsuccessful vendor (B3) did not get very polite treatment from RAL contracts – bad for any future relationship l Could we do more in house in the future? To an outsider, the EC approach looked attractive. Most composite manufacturers struggle with engineering work outside their range of experience – eg machining, assembly, jigs and fixtures »We could do these parts more effectively at RAL or in University Community l Companies that work the way we do are very few and far between

5 A.Nichols CLRC5 SCT TE Close-Out Detail technical issues l We should not have been persuaded by Lola to abandon the rigid joint rail at the OTE-side panel interface. The resultant solution was too flimsy and too difficult to seal »RAL could have machined the rails and supplied them to Lola along with a suitable bonding jig l All clearance holes were too small for what was a flimsy structure »Although the end panels fitted during the dummy assembly, the holes had to be enlarged at the final assembly – embarrassing again! l Despite the aluminium bulkhead’s huge cost and mass, it made a nice rigid circular datum for the OTE l The OTE circular flange should have been reinforced by more plies, or a metal backing ring – it was only just stiff enough to support the seal

6 A.Nichols CLRC6 SCT TE Close-Out l The screws and captive nuts were generally too small. We should have accepted M4 as a minimum size and changed designs to accommodate them if necessary l Stainless steel should have been used instead of aluminium for screws and nuts l The outer skin of the end-panel would have been better made from one piece, incorporating the PST wire channels, instead of four »Better G&S integrity »Fewer parts and therefore joints »Lower cost l More use should have been made of jigs for assembly and drilling, eg, the ITE fiasco could have been avoided by using a simple fixture to position the end rings

7 A.Nichols CLRC7 SCT TE Close-Out Assembly Issues l Much time was wasted filing the RAL-made service feedthro’s to fit the grooves – problem with the cutter radius in the corners – no problem with the UCL ones l The assembly went OK in general, but was too hurried: »A seal was left out of the ITE-end panel junction at one side »More time should have been spent understanding the problems with LMT sealing instead of pushing ahead at all cost, eg the LMT bunches needed clamping rigidly outside the TE. Some were allowed to slide inwards, which may have compromised the final position of the PPB1 connection on the harness

8 A.Nichols CLRC8 SCT TE Close-Out Step one: CFRP Mould tool manufacture This gives matched CTE during Cure – essential to meet our tolerances A steel tool would have been much cheaper But tolerances might have been more difficult - food for thought……

9 A.Nichols CLRC9 SCT TE Close-Out OTE half-cylinder, With pyrogel in place, before outer Skin is fitted Completed ITE

10 A.Nichols CLRC10 SCT TE Close-Out Side and end panels Bulkhead

11 A.Nichols CLRC11 SCT TE Close-Out OTE and side panels in situ during 4-barrel assembly at CERN

12 A.Nichols CLRC12 SCT TE Close-Out The services nightmare All these services had to pass Through the bulkhead Never again!


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