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BIRLA CELLULOSIC , KOSAMBA, GUJARAT

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Presentation on theme: "BIRLA CELLULOSIC , KOSAMBA, GUJARAT"— Presentation transcript:

1 BIRLA CELLULOSIC , KOSAMBA, GUJARAT
WELCOME TO CASE STUDY PRESENTATION ON DOWN TIME REDUCTION AT DRYER#1 By Team : GOAL BIRLA CELLULOSIC , KOSAMBA, GUJARAT

2 CONTENTS Prioritization of root cause Unit introduction
Team Detail Meeting detail Identification of Problem Selection of Problem Definition of Problem Analysis of Problem Process flow diagram Brain Storming Cause and effect diagram Prioritization of root cause Data Collection and analysis Problem faced if any Trial result Before & After sketches Action taken / Team working Cost Involved Results achieved Sustenance of result Acknowledgement

3 UNIT INTRODUCTION Name of the Unit : BIRLA CELLULOSIC
Location : Kharach , Gujarat Year of Commissioning : 1997 Installed Capacity : 77 TPD Viscose Staple Fibre 200 TPD H2SO4 (Sulphuric Acid) 24 TPD CS2 (Carbon di Sulphide) Present Capacity : 175 TPD Viscose Staple Fibre 200 TPD H2SO4 48 TPD CS2 Main Products : Viscose Staple Fibre,H2SO4,CS2 Value Added Products : Sodium Sulphate

4 UNIT INTRODUCTION Prestigious Awards Bagged in Last Two Years :
Deming Quality Award (Japan) Aditya Birla Group’s Highest Award (Gold Medal) for Manufacturing Excellence CII-Exim Bank Award for Business Excellence Rajiv Gandhi National Quality Award-Best of All Certifications: ISO 9001: 2000 ISO 14001

5 BIRLA VISCOSE’s GLOBAL PRESENCE
Grasim India Total Capacity 685 TPD Birla Cellulosic, Total Capacity 175 TPD Spread of multi unit operations places us in a unique position to offer to our customers price competitive viscose fibre

6 OUR MARKET LEADERSHIP POSITION
Birla Cellulosic’s World Market Share = 4 % AV Birla Group has almost 100% market share in India.

7 TEAM DETAIL Meeting Day : Tuesday , Meeting Time : 3:30 PM
Ownership Area : Spinning , DCS Team formation date : TEAM MEMBER RESPONSIBILITY Sudhansu Jain ( Leader) To Provide Resources and Guidance Manoj Patwari ( Dy. Leader) Co-ordination with Process personals & Implementation of action plan Kamal Kak Data analysis & Use of PS Tools Omkar Yadav Data analysis & Use of PM Tools Vijay Atodaria Equipment Study and Execution of Instrument Jobs Jitendra Adwan Data analysis & Use of PS Tools Deepak Patel Equipment Study and Co-ordination during machine shutdown Hemant Patel Analysis of Trial implementation and Implementation of action plan

8 MEETING DATE / ATTENDANCE

9 MILESTONE CHART

10 IDENTIFICATION OF PROBLEM
Category 1 To reduce the dept book stock inventory level from 21 lacs to 15 lacs B 2 To reduce the surplus material stock at yard and wear house 3 To identify the obsolete material and arrange to selling 4 To initiate ARC of consumable items to reduce cycle time in procurement 5 To transfer the ARC instrument items at stores to release the PO from store to reduce the lead time 6 To increase the % Skill level of technician from 65% to 85% 7 Training to Instrument technician for electrical jobs 8 Training to Electrician for Instrument related jobs 9 Training to bailing press operators for alarm details A 10 To cover all team members for KIP tours at different units “A”: To be solved by Team, “B”: Other department help required, “C”: Management decision required

11 IDENTIFICATION OF PROBLEM
Category 11 Training to technician for PDCA cycle approach B 12 Down time reduction at DRYER#1 A 13 To reduce the moisture variation at Dryer#2 due to improper logic at DCS as per viscose flow 14 Down time reduction in Spinning machine #1 due to DO card 15 Identification of critical loops for redundancy 16 To increase the % nos of Critical instruments from 42 to 65% 17 To include more nos of repeating problems in PM schedule 18 To reduce the down time of Dryer#2 control valve 19 Overload tripping of Sumpzone pumps 20 To reduce failure of DCS cards by corrosion on the tracks C “A”: To be solved by Team, “B”: Other department help required, “C”: Management decision required

12 IDENTIFICATION OF PROBLEM
Category 21 To reduce M/c#2 freq drive card failure due to corrosion C 22 To increase the nos of Kaizen from 1.8 nos/member to 4 nos / member / year B 23 Steam leakages from the control valve galndes 24 Cable insulation failure at the line#2 PU cables 25 Magnetic flow meter card / senor testing for fluctuation in reading 26 To reduce the chronic problem of PU tube failure at cutter A 27 To modify the system for DCS data display at Forte screen 28 To remove the unwanted looping in dryer panel / MCC 29 To implement the kaizen for use of PT as level transmitter 30 To reduce the Panel view failure of bailing Press “A”: To be solved by Team, “B”: Other department help required, “C”: Management decision required

13 IDENTIFICATION OF PROBLEM
Category 31 To reduce the high bale weight problem in bailing press B 32 Interfacing of Siemens PLC data on DCS of Prepress bale ready pressure 33 To identify the unnecessary / Obsolete items in the dept A 34 Non availability of standard labelling in the inventory room 35 Muda in Bottlenecking at DCS APM#11,13 side C 36 Muda in inventory of control valves 37 Muda in motion for Store room key 38 Muda in communication for DCS data on common LAN 39 To reduce the retrieval time form 6 min to 1 min 40 To eliminate Muda in Untidiness at DCS marshalling cabinet side multi core cabling “A”: To be solved by Team, “B”: Other department help required, “C”: Management decision required

14 IDENTIFICATION OF PROBLEM
Category 41 To improve 5s score of ownership area form 75% to 95% B 42 Muda in untidiness at Logic manger # 17, 19 C 43 Muda in bottlenecking at LM#19 44 To create space in marshalling panel by removing unwanted signal splitter A 45 To improve file labelling level in filing cabinet 46 Higher stationery consumption in department 47 To improve the office 5s score form 78 to 85 % 48 Lack of awareness regarding safety precautions while working at CS2 line 49 Lack of awareness regarding the preventive measures while working at steam line 50 To reduce the failure of pH sensor for soft finish “A”: To be solved by Team, “B”: Other department help required, “C”: Management decision required

15 IDENTIFICATION OF PROBLEM
Category 51 To reduce the CV for desulph bath temperature from 3.3 to 0.5 B 52 To reduce the CV for bleach bath temperature from 2.2 to 0.5 53 To reduce the CV for soft finish bath temperature from 1.7 to 0.5 54 Poor visual display about the spare channels at DCS A 55 Poor display of DO RTP details on the marshalling panel 56 To display the 24 VDC power supply looping on the marshalling cabinet 57 Poor display of MCC wise motor details in substation 58 Deletion of unwanted tags in Spinning section (APM#13) 59 To analyse top 100 consumable items to reduce its consumption. 60 To develop substitute for imported speed indicators of REXROTH machine “A”: To be solved by Team, “B”: Other department help required, “C”: Management decision required

16 CATEGARISATION OF PROBLEM ( PIE CHART)
CATEGORY A B Total numbers of problem Identified 60 Total numbers of problem solved 17

17 PROBLEM SELECTION IN CATEGORY ‘A’ ( By Voting )
Criteria : 16 No. for Highest priority, 1 No. for lowest priority ( Separate No for each Cause )

18 PROCESS FLOW DIAGRAM Any problem in dryer results in : VISCOSE
SPINNING MACHINE AFTER TREATMENT DRYER BAILING PRESS AUXILIARY Any problem in dryer results in : 1. Production loss due to slow run of Spinning machine 2. Adverse effect on quality of fiber

19 FIBER FLOW IN DRYER Dryer Sequence : Dryer Interlocking :
To Bailing press From After treatment Drum Drive#3 Drum Drive#2 Drum Drive#1 Nip roller Doffer Wet Feeder Horz. Conveyer Zero Speed switch ExhaustFan Motor Dryer Sequence : Dryer Interlocking : Start all the fans Start Drum Drive #3 ,2,1 Start Nip roller Start Doffer Start Wet feeder Start Horizontal conveyor If any exhaust fan stops, complete dryer will stop If any drum drive zero speed switch senses zero speed, Dryer Sequence will stop including that drive and Horizontal conveyor will run in reverse mode

20 DEFINITION OF PROBLEM This improvement project is related to “KAIZEN” Sub Committee to reduce the Down time. Down time from 6-7 Hour to 0 hour/year Tripping frequency from 18 to 0 Nos/Year Production loss from 5.3 tons to 0 Tons/Year Yellow Patches bale generation from 36 bales to 0 bales/Year

21 ANALYSIS OF PROBLEM / DATA
FROM APRIL-02 TO JULY-02 FROM LOG BOOK : No Shift Nos of occurrence Down time (Minute) Average Down Time / Problem 1 G 4 80 20 2 A 17 3 B 45 22.5 C 105 35 Average down time / Problem : 24.7 minutes

22 ANALYSIS OF PROBLEM 1. Dryer#1 was stopping due to malfunctioning of zero speed switch 2. For identifying problem dryer has to restarted again and stopped to solve the problem due to which down time was increasing. 3. In B&C shift if E&I technician is busy in some remote location down time was increasing 4. For each stoppage of Dryer#1, 2 nos of SYP bales are generated which was direct loss due to yellow patches 5. For starting the dryer one fan was physically stopped to restart the sequence which was not advisable for motor 6. Attention from the main problem is diverted and main concentration is on zero speed switch 7. If there is any problem in zero speed switch and transmitter has not sensed correctly 2 to 3 hour breakdown may occur

23 BRAIN STORMING FOR CAUSE IDENTIFICATION
Team No: 44L102, 44L101, 20L104 No CAUSES SUGGESTED BY 1 Targets for the switch are not proper at drive shaft J Jadav 2 Support for mounting the switches are loose S Rajput 3 Long procedure to attend the switch problem M Patwari 4 Zero speed switch cables damage due hot air from dryer doors J Adwan 5 Non availability of redundant system at drum drives critical location to avoid breakdown 6 No provision to start the dryer sequence without stopping the fan S Jain 7 No indication of zero speed switches on dryer graphics at DCS M Patel 8 Proximity switches are not tightened with proper tool S Garg

24 BRAIN STORMING FOR CAUSE IDENTIFICATION
Team No: 44L102, 44L101, 20L104 No CAUSES SUGGESTED BY 9 Use of NO contact for drum dryers at DCS RTP M Patwari 10 Power supply to zero speed transmitter is given from lighting DB M Dubey 11 Non availability of proper JB Schedule to reduce the down time Nalin Parmar 12 No visual indication of switch to provision to check the healthiness of Proximity switches Omkar Yadav 13 Loose contact of cable at the marshalling cabinet Hemant 14 Cable glands are nor proper at the transmitter end Omkar 15 No interlocking of dryer with after treatment low pressure to avoid jamming at drum PN Murli 16 Fiber jamming between the drums Deepak 17 Poor sensing of proximity switch Vijay

25 BRAIN STORMING FOR CAUSE IDENTIFICATION
Team No: 44L102, 44L101, 20L104 No CAUSES SUGGESTED BY 18 Power supply is not regulated M Patwari 19 Poor quality of zero speed switch Kamal 20 Poor quality of zero speed transmitter 21 Corrosion at the DCS cards Omkar 22 Corrosion at the cable terminals J Adwan 23 While working fuse is not removed for transmitter Vijay 24 Gap is varying between switch and target 25 Zero Speed transmitter sensitivity knob is at low side S Garg 26 Switches are not tightened with proper tool Hemant Poor interlocking wrt Aftertreatment#1

26 CAUSE & EFFECT DIAGRAM FOR DRYER#1 , PROJECT
Method Non availability of redundant zero speed switch at the drum drive end 1 Non Availability of redundant system : Root Cause Switches are not tightened with proper tool due its non availability : Cause 2 Cable glands are not proper at transmitter Check nut of switch are getting loose 3 No Bypass facility to attend the problem No provision to start the sequence without stopping the fan Long Procedure to attend the problem DRYER#1, Down time increases

27 CAUSE & EFFECT DIAGRAM FOR DRYER#1 , PROJECT
Method Transmitter sensitivity knob is at higher scale Poor sensing of proximity switch : Root Cause 4 No of target / rotation is less : Cause Gap varies between target and sensor No interlocking at DCS with AFT#1 low Oil pressure 5 Use of NO contacts at DCS for Drum drives Fiber jamming between drums Zero speed switch cable covering is done for protection 6 Zero speed switch cable damage due to hot air or maintenance work DRYER#1, Down time increases

28 CAUSE & EFFECT DIAGRAM FOR DRYER#1 , PROJECT
Material 7 LED type proximity switch is not used : Root Cause No Visual indication on the Switches : Cause Poor quality of zero speed switch Poor quality of zero speed transmitter Corrosion at the cable terminals Marshaling panel is not sealed 8 Corrosion at the DCS card DRYER#1, Down time increases

29 CAUSE & EFFECT DIAGRAM FOR DRYER#1 , PROJECT
Machine Mounting support of switch is getting loose : Root Cause 9 Vibration in the drum drive shaft : Cause Gap between switch and target varies Power supply is given through Lighting DB 10 Power supply is not regulated Spikes in the power supply of transmitter DRYER#1, Down time increases While working power supply is not switched off 11 Non Availability of JB schedule Man

30 PRIORITIZATION OF ROOT CAUSES ( By RPN No. )
Scale for “S”: 1 to 10: Scale for “O”: 1 to 10, Scale for “D”: 1 to 10,

31 PRIORITIZATION OF ROOT CAUSES
PARETO ANALYSIS Cumulative Root Cause

32 FROM AUG-02 TO AUG-03 FROM LOG BOOK :
DATA COLLECTION FROM AUG-02 TO AUG-03 FROM LOG BOOK :

33 DATA ANALYSIS Average down time / Problem : 20.5 minutes No Shift
SUMMARY OF DATA COLLECTION FROM AUG-02 TO AUG-03 : No Shift Nos of occurrence Down time (Minute) Average Down Time / Problem 1 G 6 85 14 2 A 3 63 21 B 5 102 20 4 C 111 28 Average down time / Problem : 20.5 minutes

34 PROBLEM FACED IN IMPLEMENTING THE PROJECT
No Problem faced Action taken 1 Multi core cable limitation at field JB from DCS as only one spare pair was available 24 Vdc Bus made in JB and common supply given from JB instead of from DCS 2 Branch cable requirement from Junction box to transmitter for redundant switch Spare core of existing branch cable is used 3 6 nos of redundant 2 wire proximity switch required for drum drive Removed proximity from GCF is used ( Given by team 44L101 ) 4 Budgetary problem of Zero speed transmitter for new switches (6 Nos ) Feed back is taken to DCS and sensing of zero speed is done at DCS without transmitter

35 Average down time / Problem Average down time / Problem (Min)
TRIAL RESULT DCS : Bypass facility at DCS to restart the Dryer #1 and finding Problem Modification Date : Average down time / Problem BEFORE DURING TRIAL Average down time / Problem (Min)

36 Numbers of Occurrence graph at DrumDrive#1, Right side
TRIAL RESULT Location : Drum Drive#1, Right side extra new redundant proximity switch installed Modification Date : Numbers of Occurrence graph at DrumDrive#1, Right side BEFORE DURING TRIAL Nos of Occurrence

37 BEFORE / AFTER SKETCHES
Proximity Target Drum drive shaft BEFORE Proximity Switch Switch support New Proximity Switch New both side target AFTER Proximity Switch Switch cable through PVC conduit

38 ACTION TAKEN / TEAM WORKING

39 ACTION TAKEN / TEAM WORKING

40 MILESTONE CHART

41 COST INVOLVED IN IMPLEMENTING THE PROJECT
No Material required Qty Projected Cost Action taken Implemented Cost 1 Proximity switch 6 Nos 5400 Removed proximity from GCF is used 2 Multi core cable from DCS to JB ( 6 Pair X 0.75 Sqmm) 225 mtr 22500 24 Vdc Bus made in JB and Spare cable used 3 Branch cable from JB to Zero speed switch 180 mtr 9000 Spare core of 3 core cable used 4 Digital input channel 7 Nos 12000 New Digital input card installed 5 New switch support welding 1 gang 600 Support modified at work shop and welded with M/s JN associate gang 6 Zero speed transmitter 30000 TOTAL 79500 12600

42 Numbers of Occurrence / Month Nos of Occurrence/ Month
RESULTS ACHIEVED Numbers of Occurrence / Month BEFORE AFTER Project Completed Nos of Occurrence/ Month Root Cause

43 RISK PRIORITY NUMBER ( RPN ), After Implementation
RESULTS ACHIEVED RISK PRIORITY NUMBER ( RPN ), After Implementation

44 RISK PRIORITY NUMBER ( RPN )
RESULTS ACHIEVED RISK PRIORITY NUMBER ( RPN ) RPN Number Root Cause

45 RESULTS ACHIEVED Average Down Time / Problem (Minutes)
BEFORE DURING IMPLEMENTATION AFTER Project Completed Average down time / Problem (Min)

46 RESULTS ACHIEVED No Detail Before After 1 Breakdown time 361 minute
( Aug-02 to Mar-03) After ( Apr-03 to Aug-03) 1 Breakdown time 361 minute 0 minute 2 Frequency of occurrence 18 Nos 0 Nos 3 Numbers of Yellow patches SYP bale generation 36 Nos 4 Production loss due to slow run of machine 5.3 Tons 0 Tons 5 Proximity switch failure 3 Nos 1 Nos 6 Average Down time / Problem 20.05 Min 0 Min

47 BENEFITS Tangible benefits : Intangible benefits : No SAVING RUPEES 1
Fiber production loss due to slow run of machine ( 5.3 * ) 3,44,500 2 Proximity switch consumption ( 3 * 1000 ) 3,000 3 Reduction in Yellow patches bale (36*2500 ) 90,000 TOTAL ( Rs/ Year) 4,37,500 Intangible benefits : Low quality bale due to Yellow patches is reduced Confidence on the Dryer interlocking is increased ICSI index is increased from 75% to 95% Inventory of the zero speed transmitter is made zero.

48 SYSTAMATISE THE PROCESS Preventive Maintenance Checklist
SUSTAINANCE OF RESULT SYSTAMATISE THE PROCESS No CAUSE COUNTER MEASURE SOURCE 1 Tightness checking of proximity switch Switch check nut loose at support Daily Checklist 2 Gap checking between target and zero speed switch Gap between sensor and target should be < 10 mm Preventive Maintenance Checklist 3 Proximity healthiness checking LED indication on proximity switch and Green indication on graphics 4 Malfunctioning of zero speed switch Alarms on DCS 5 Delay in attending the problem Time in attending the problem Training

49 SUSTAINANCE OF RESULT

50 ACKNOWLEDGEMENT We acknowledge our sincere thanks to team of Spinning for their valuable suggestion during Brain Storming session and their support during execution of our project. We are thankful to HOD-E&I for pondering the responsibility and support for taking up the project. We are thankful to Vice President (Technical) for his valuable suggestions and support during execution of our project.

51 Thank you..

52 We Welcome your Suggestions & Questions


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