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Published byÉΘεοκλής Σαμαράς Modified over 6 years ago
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SYED MUHAMMAD ALI NAQVI (Management Associate)
Presentation Losses Control at DAP PLANT Presented by: SYED MUHAMMAD ALI NAQVI (Management Associate)
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Purpose To reduce the losses and recover into system for optimizing Plant Process
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Scope of Presentation Background Losses at DAP Plant
Losses Emission Points Reasons, Effects and Recovery of Dust Loss Reasons and Recovery of Ammonia Loss Stack Losses and comparison of Design & Operating conditions Suggestion
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Background In any Process industry, Loss of Nutrients (either from Raw material or Product) is the Loss of Money, Loss in Profit and mitigation of Production rate.
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Losses at DAP Plant Losses at DAP Plant Dust Lost P2O5 Loss
Ammonia Loss P2O5 Loss
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Losses Emission Points
Ammonia Loss Dust Loss Stack Dedustig Section Scrubbing Section Polishing Screens Gaseous Ammonia GPR Granulator Primary Screens Scrubbing Liquor Phosphoric Acid H2SO4 Dryer Product Conveyor Liquid Ammonia F.B.C Pre neutralizer Polishing screen feed elevator Oversize Crusher Coater Primary Screen Feed Elevator Chilled Air Recycle Solids Granulator feed bucket elevator Recycle Belt Conveyor
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Reasons of Dust Loss Quality of Phosphoric Acid
Limitation of Dedusting Section
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Effect of Dust Emission
Continuous reclaiming of dust Housekeeping
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Dust Recovery Dusty gases from Dryer Bag house Granulator
Dryer Venturi Scrubber Dust Recovery Dusty gases from Dryer Instrument Air Dryer Exhaust Fan Dryer Dedust Cyclone Bag house Hopper Dusty air from Conveyors, Elevators, Screens Dust Dedusting Exhaust Fan Dedust Cyclone Granulator Hopper Recycle Belt (DM-223)
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Reasons of Ammonia Loss
Frequent Shutdown & startup Reasons of Ammonia Loss Poor working of Scrubbing
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Schematic diagram for Ammonia Recovery
Atmosphere Above 90%NH3 recovered PN & Granulator Gases From Dryer exhaust fan STACK 50-70 %NH3 recovered Above 95%NH3 recovered TAIL GAS SCRUBBER RG SCRUBBER PRE-SCRUBBER Industrial Water Maximum NH3 recovered Dryer SCRUBBER H2SO4 PN Reactor Phosphoric Acid PRIMARY SCRUBBER TANK
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Stack losses Component Design Loss Actual Loss in 2011
Actual loss during 2012 Particulate matter 150 mg/NM3 <10 mg/NM3 Ammonia 100 mg/NM3 79 mg/NM3 73 mg/NM3 P2O5 36 mg/NM3 Fluoride 30 mg/NM3 <1 mg/NM3
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Suggestion Good quality of Phosphoric acid should be used.
Size of flappers of Dedusting hoppers should be increased for increasing suction of Dedusting Fans for lowering emission of dust in operating area. Scrapper system of Recycle belt (DM-223) should be maintained properly. Provision of Dual strainers in the discharge of RG scrubber Pump(DP-5012).
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Thank You
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Comparison of Stack Dust Loss(mg/NM3) b/w Operating & Design conditions
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Comparison of Stack Ammonia Loss(mg/NM3) b/w Operating and Design Conditions
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Comparison of Stack P2O5 Loss(mg/NM3) b/w Operating and Design Conditions
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Dedust cyclones and Bag house Analysis
Equipment Date Component Unit Inlet Duct Outlet Duct DD-431 26/4/12 Dust g/NM3 906 6 DD-4032 408 4 DD-433 322 8 Bag House 5 .04
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Phosphoric Acid SHIPMENTS
Composition: Range th th th th P2O – Fe2O – Al2O – F – CaO – MgO –
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Analysis of three types of phosphoric acid produced by acidulation of different phosphate rocks
Item Acid A (wt%) Acid B (wt%) Acid C (wt%) P2O Fe2O Al2O F CaO MgO
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Comparison of the effects of impurities on the number of
fine particles and granulation quality of produced DAP
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Operating Range of Scrubbing Section
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