Continuous Run in May 2013 2013.05.29 K.Kubo. Final Focus Test Line IP; ~40 nm beam ATF Linac (1.3 GeV) ATF Damping Ring (140 m) Extraction Line Photo-cathode.

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Presentation transcript:

Continuous Run in May K.Kubo

Final Focus Test Line IP; ~40 nm beam ATF Linac (1.3 GeV) ATF Damping Ring (140 m) Extraction Line Photo-cathode RF Gun Focal Point Accelerator Test Facility (ATF) at KEK

Strategy of the 2 weeks Achieving (confirming) small beam size at low intensity is the top priority Optics 10x1 Try all knobs Other important issues to be studied Wakefield study – Effect of bellows hields. – Studies using bellows on mover Emittance in extraction line More reliable IP beam size measurement

Procedure Scenario of 2013 May continuous operation (by T. Okugi in meeting 2013 May 10) 1) DR tuning and optimize the frequency. ‐ tuned on the DR orbit FB?? 2) EXT tuning ‐ orbit, dispersion and coupling tuning. ‐ emittance measurement ( if we can not use OTR3X, we measure the emittance OTR0‐2X and MW3X). ‐ matching to FF. 3) IP beam size measurement with MWIP ‐ IP horizontal dispersion correction by changing QF1FF. ‐ IP horizontal waist optimization by changing AX knob. ‐ IP vertical waist optimization by changing QD0FF. ‐ BBA of sextupoles and tuned on the sextupoles. 4) Startup the IP‐BSM ‐ Linear knob optimization by 2‐8 deg. mode ‐ Linear knob optimization by 30 deg. mode ‐ Beam orbit was set and optimize the mover bellows to be small intensity dependence of IP beam size. ‐ tuned on the FF orbit FB. ‐ Linear knob optimization by 30 deg. mode again. 5) IP beam size measurement by IP‐BSM 174 deg. mode. ‐ Fringe tilt & pitch optimization ‐ Linear and nonlinear knob tuning

Continuous Run, May (Mon) Start and tuning 14 (Tue) Problem with Bellows Shield. 15 (Wed) Solved Wed. Day tuning 16 (Thr) Problem with Linac RF #4 Study Cancelled 17 (Fri) 18 (Sat) High modulation 30deg -> 174 deg mod. 19 (Sun) Struggled to squeeze beam. 30deg high mod -> knobs 174deg -> lost mod. -> back to 30deg 30 deg tuning was quick. ~70 nm not difficult, mimimum ~60nm 20 (Mon) 21 (Tue) 22 (Wed) 23 (Thr) Change optics (betax* and betay*) 24 (Fri) Intensity dependence, etc.

Bellows shields inserted Shields were inserted for most of bellows in high-beta region in May 2013.

Troubles with bellows shield Found and removed Wed., May 15.

Big daily temperature change in sunny days Machine was not very stable (DR circumference change) Graphs from Japan Meteorological Agency May 19May 20 May 22 May 21 May 23May 24

1:00~9:009:00~17:0017:00~25:00 13 (Mon) Kubo 14 (Tue)KurodaTauchi, (Okugi)Okugi, A 15 (Wed)White, BTauchi, CKuroda, D 16 (Thr)Cancelled 17 (Fri)Cancelled 18 (Sat)CancelledKubo, DTerunuma, A 19 (Sun)Okugi, BTauchi, CWhite, D 20 (Mon)Kubo, AOkugi, BKuroda, C 21 (Tue)White, DMarin, AKubo, B 22 (Wed)Kuroda, COkugi, DWhite, A 23 (Thr)Kubo, BKuroda, CMarin, D 24 (Fri)Terunuma, White, AKuroda, Okugi, B Study leaders: Okugi, Kuroda, Kubo, White, Marin, Terunuma, Tauchi Sub leaders: A: Young-Im Kim, Janice Nelson B: Sha Bai, Shan Liu C: Yves Renier y, Juergen Pfingstner, Andrea Jeremie(1 st week) D:Neven Blaskovic, Jacqueline Yan, Robert Ainsworth Study Shift

Emiitance in Extraction Line (multi-OTR monitors) QS magnets were used for coupling correction. We had used only QK magnets before. QSs had been used only for dispersion correction. Strength o f QK magnets significantly reduced. QS: upstream of EXT line, in dispersive region QK: Just before beam size measurement. Dispersion free region. Rotation of OTR monitor Adjusted Vertical emittance ~13 pm at N=6e9 ~10 pm at low intensity Improved

Examples of 174 deg mode fringe scans Beam size ~ 60 and ~ 90 nm Preliminary

Intensity dependence Modulation (30 deg.) vs. intensity for different betax* and betay* Almost the same dependence for all cases, a=20nm/1e9 This is slightly larger than in April. Orbit dependence was not systematically studied yet. Fitting By T.Okugi One exception?

Intensity dependence Examples of modulation (30deg) vs. intensity Only this scan shows weak dependence. Others are all similar.

Modulation (30deg) vs. position of on-mover bellows Example Peak was observed

Ref. Cav. Bellows Ref. Cav. Bellows Shielded Bellows Shielded Bellows Dec.2012 May 2012 Dec.2012 – April 2012 on-mover wakefield source Bellows

1 Bellows +2 shielded bellows for movement : nm/mm/1e9 2 Ref. Cavities +2 bellows for movement: 27-28nm/mm/1e9 1 Ref. Cavity +2 bellows for movement:14-19nm/mm/1e9 Modulation (30 deg) vs. position of bellows Studies using on-mover wakefield source By T.Okugi

Tuning knobs Corrected coupling Linear knobHorizontal move of sextupole magnets yy’ vertical move of sextupole magnets Ey x’y Non-linear knob Strength change of sextupole magnets x’yy’ Eyy’ Strength change of skew sextupole magnets xxy Exy EEy yy’y’ 5 sextupole magnets (on mover), 4 skew-sextupole magnets

Effect of Non-linear knob Most non-linear knob scans were not effective. Very few exceptions. (Effective just because linear knob scan was not optimized??) Could not find effective skew-sextupole knobs scan. (?) Change sextupoles strengths)

Conclusion of the weeks (1) Small beam size at low intensity? – Repeatedly achieved < 70nm beam size at low intensity by tuning, and kept hours. – Minimum beam size ~60nm – Could not reduce further Multi-pole field – We did not see clear effect of the skew-sextupole correctors.

Conclusion of the weeks (2) Wakefield – Effect of bellows shield was not clear. Intensity dependence did not reduced. – Cannot explain beam size growth 40nm -> 60nm at low intensity (N~1e9) Similar intensity dependence for different betax* and betay*, suggesting dependence is from wake field, not from multi-pole field. Emittance in Extraction Line – Improved. Vertical emittance about 10 pm (low intensity) ~ 13 pm (N~6e9), weak intensity dependence. – Coupling correction in upstream part – Tuning of OTR monitor