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Published byAdele Potter Modified over 8 years ago
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TCA and Contributions Made to Improve SMC Paintability
Mike Siwajek ThyssenKrupp Budd Company Society of Plastics Engineers Automotive Composites Conference September 9-10, 2003 Troy, MI
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Goals and Objectives
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Defect Root Cause Analysis
500+ defects from 10 assembly plants catalogued Large percentage of defects due to microcracks from handling Majority of “handling” defects occurred after primer application
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Root Cause Breakdown Cracks & damage
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Toughening the Matrix Targeting edge defects Evaluate all components
resins fillers LPA’s additives catalysts / inhibitors glass
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Improved Toughness TCA Control
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Paint Pop Flex Test 2 x 18 x 0.1 test strips
8.25 diameter cylindrical mandrel designed for 125% of ultimate stress deformation creates micro-cracks on SMC surface Paint with conventional Primer-sealers using E-coat bake simulation (380F for 30 min.) count “paint pops” on surface of SMC
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PP Flex Test Panels Control Tough Class ‘A’
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Verifying TCA’s Effectiveness
Multiple DOEs performed Ford Paint on Plastics Team / 6-sigma black belts AOC Red Spot Studied effects of SMC type Humidity E-coat Stress after molding (molding plant damage) Stress after priming (body shop handling damage) Type of primer (standard 2K and UV Thermal)
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TCA DOE Results TCA less affected than control
Sample Paint Pop Test Results TCA less affected than control humidity temperature handling extremes 90+% improvement in pop resistance over control Desired
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TCA Implementation TCA has afforded:
Conversion from double layer of primer to single layer of primer without degradation in quality Up to 98% reduction in paint defects Currently less than 10 defects submitted for microscope analysis (since May 2002) - Zero Microcracks
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Ford Sport Trac Process DOE completed in May 2002 (defect rate reduced to ~60) Full conversion to TCA in June 2002 Defect rate has dropped from ~60 to below 10
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Ford T-Bird Defect rate includes all parts fender converted July 2002
decklid 07/29/02 hood 09/2002 Level defect rate for TCA 1X primed vs standard SMC 2X
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Ford Ranger Hood Full conversion to TCA 08/13/02
Defect rate dropped from ~200 to nearly 0 Pop rate data collection suspended by assembly plant Conversion to TCA
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Lincoln Navigator Hood
Converted hood to TCA on 06/17/02 Level defect rate for TCA 1X primed vs. standard SMC 2X
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Lincoln Navigator Fenders
Converted fenders to TCA August / September ‘02 Level defect rate for TCA 1X primed vs. standard SMC 2X
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Paint pop Data Collection Suspended
Ford Mustang Hood Terminator, GT Hoods and Decklid converted to TCA Defect rate reduced to 0-20 Mach 1 launched with TCA Paint pop Data Collection Suspended by Assembly Plant
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Paint pop Data collection suspended
Ford Mustang Decklid Paint pop Data collection suspended by assembly plant
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Ford Econoline Hood Converted to TCA February 2003 Conversion to TCA
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What next??? Remove the Class ‘A’ SMC Stigma at OEMs
Tough Class ‘A’ UV Thermal Primer New primer-sealer technologies SMC Consistency Program Best practices (compounding and molding) Defect traceability Eliminate variability
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SMC Consistency Improvement Plan
Target programs for improvement Identify Key Performance Criteria (KPCs) as defined by customer (molding plant or OEM) Target broad cross-section of causes for inconsistencies (Control Factors / CFs) Form cross-functional teams to focus on this effort Stepwise regression of defects vs. CFs Develop a sound engineering basis for the effort
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SMC Consistency Roadmap
Data Analysis - identify Data Gathering possible CF's Brainstorm - understand failure mode failure mode identified ? no yes Conduct experiments to Implement in production verify failure mode Establish CF statistical Data Gathering to verify capability improvement
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Acknowledgements SPE Ford GPE AOC Red Spot TK-Budd Team
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