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The 2 nd annual Air-Cooled Condenser User’s Group Meeting WenhuaTian Huiyong He Xi’an Thermal Power Research Institute Co Ltd.(TPRI), China September 28-29,

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Presentation on theme: "The 2 nd annual Air-Cooled Condenser User’s Group Meeting WenhuaTian Huiyong He Xi’an Thermal Power Research Institute Co Ltd.(TPRI), China September 28-29,"— Presentation transcript:

1 The 2 nd annual Air-Cooled Condenser User’s Group Meeting WenhuaTian Huiyong He Xi’an Thermal Power Research Institute Co Ltd.(TPRI), China September 28-29, 2010 Pueblo Air-Cooled Condensate Polishing in China

2 CONTEXTS I. Introduction of TPRI II. Developments of ACCs in China III. Carbon Dioxide in ACCs IV. DO Controlling in ACCs V. Case of Indirect ACCs

3 Introduction of TPRI

4 Developments of ACCs in China

5 Outline The distribution of coal and water resources in China is asymmetric; coal-rich regions typically lack water and vice versa Because of its significant water-saving advantage, ACC is suitable for drought-prone regions in northern China. So the government of China required that all the new built coal power plants should be used ACCs in drought- prone regions after 2002 The use of ACCs has increased rapidly in China within the past five years

6 Development of ACCs The total capacity of ACCs was about 24,000MW by 2007 The percentage of ACCs was 4.3%(Total capacity of coal power plant was 554,000 MW ) The number of constructing sub-critical ACC plants was 47, and the capacity was 46,000 MW (2008 ~ 2009) Number o f units Capacity(MW) Total Capacity(MW) 2360013,800 253007,600 112002,200

7 It is estimated that the total capacity will reach 1,200,000MW until 2015 in China Capacity of coal power plant will be 820,000MW Capacity of ACCs will surpass 100,000MW and occupy 12% Foreground

8 Direct ACCs were the majority, occupied 93% in 2007 Indirect ACCs developed rapidly after 2008. Up to now, the operation capacity is 4,200MW, and other units with 16,800MW capacity is constructing Ratio of Direct & Indirect

9 The percentage of different CPP(2009)

10 Direct ACCs were the majority, occupied 93% in 2007 Indirect ACCs developed rapidly after 2008. Up to now, the operation capacity is 4,200MW, and other units with 16,800MW capacity is constructing Ratio of Direct & Indirect

11 Dalater Power Plant ( 4×600MW,Inner Mogolia )

12 Powdered resin filter

13 Datang Tuoketuo Power Plant ( 4×600MW,Inner Mogolia )

14 Unit 5 high-speed cation bed

15 eparated bed in Jingjie power plant ( 4×600MW, Shaanxi ) Separated bed in Jingjie power plant ( 4×600MW, Shaanxi )

16 Carbon Dioxide in ACCs

17 Analyzer method & Instrument Because carbon dioxide in high pure water such as condensate is as low as μg/L(ppb) level, it is difficult to sample and determine. Trace carbon dioxide analyzer(Sentry Co. ) can measure carbon dioxide in high pure water as low as ppb level on- line. Advantages: (1) convenient and quick testing process (2) high accuracy, good repeatability and high sensitivity Standard: D 4519-94 ( Reapproved 2005 ) by ASTM

18 Trace carbon dioxide analyzer(Sentry Co. )

19 This test method measures the electrical conductivity of high purity water through a cation exchanger in the hydrogen form, then through an electric reboiler. The effluent was boiled at atmospheric boiling water temperature after acidic (volatile) gas removal. subsequently, it was cooled at 25 ℃. Passage through the cation resin replaces cations (including ammonia and amines)in the water with hydrogen ions. Two conductivity cells located in the instrument provide measurements of the cation conductivity at the incoming sample temperature, and the effluent conductivity at 25 ℃. In order to obtain the carbon dioxide, subtract the conductivity of pure water (0.055μS/cm) from the conductivity of the final effluent cell. Then deduct this value from the cation conductivity obtained from the cell immediately after the cation exchanger resin. Use this adjusted conductivity value to look up the concentration of volatiles expressed as a concentration of carbon dioxide in Table. Determination Methods

20 Tongchuan Power Plant (2×600MW,Shaanxi Province) Powdex of Tongchuan Power Plant

21 Shangan Power Plant (2×600MW, Hebei Province) CA-AN Bed of Shangan Power Plant

22 Plant Type of unit Type of condensate polishing DO in condensate ( μg/L ) CO 2 (μg/L) Fe (μg/L) pH Condensa te Effluent of polishing Feed water Condensate A Subcritical pressure drum boiler Powdex8530201515.09.4 B Supercritical Once- through boiler Pre- filtration+ CA -AN bed 2012318.09.4 Determination Results At the same pH condition, the higher level of CO 2, the higher level of Fe in the condensate CO 2 recycles in plant A, but it is removed in plant B by separated beds in plant B It is important to control the level of CO 2, it will reduce corrosion of metals in ACCs.

23 DO Controlling in ACCs

24 Determination of DO DO in condense will make iron corroded in ACCs, so the limit DO concentration is 100ppb in China The operational ACCs in condense often surpass the limit of 100ppb

25 Zhaoguang Power Plant (2×300MW+2×600MW, Shanxi Province) Yushe Power Plant (2×300MW,Shanxi Province)

26 Wuxiang Power Plant (2×600MW,Shanxi Province) Hejin Power Plant (2×300MW,Shanxi Province)

27 Determination results of DO Power PlantCapacityStart-up time DO in condensate ( μg/L ) Hejin2×3002005 70 ~ 106 Yushe2×3002004.10 85 ~ 237 Zhaoguang2×300 2005.7 ( #1 unit ) 2005.9 ( #2 unit ) #1 unit:20 ~ 55 #2 unit:52 ~ 84 Wuxiang2×6002006.10 < 30 The reason of high DO in condensate : 1. Vacuum system is too large that will lead to air leakage in ACCs. 2. DO in make-up water is too high. For example, it is 800 ppb in some power plant.

28 Methods to decrease DO Strengthen the welding management and improve its quality, try to decrease the air leakage of vacuum System retrofitting----Case Power Plant Capacity Start-up time Before the retrofitting After the retrofitting Wuxiang 2×600 MW 2006.10.6 the exhaust unit was installed out of the condensed water tank, make-up water is supply to external condensed water tank The condensate tank was combined to the exhaust air cooling device. After through the nozzle, the makeup water goes to the throat of exhaust device. It can lead to an increase of the secondary removal of oxygen in returned condensate.

29 Load ( MW ) Backpressu re ( kPa ) Flow of Make up water ( t/h ) Flow of Condensate ( t/h ) Condensate Temperature (℃) DO ( μg/L ) 36021.028.9760.961.2 < 0.5 50023.050.71045.363.2 < 0.5 60020.548.21269.460.71.2 60019.118.81240.060.00.7 DO in condensate after retrofitting

30 Case of Indirect ACCs

31 Yangcheng Power Plant is located in Shanxi province in China. The first stage project are 6×350MW subcritical WCCs , which was completed at 1997.8. The second stage project are 2×600MW subcritical indirect ACCs named SCAL, which began to construct at 2005.5.18 and completed at 2007.9. Basic Information The SCAL ACCs is produced by EGI company(Hungary), and it is more like the combination of Harmon’s no tower system and Heller’s cooling tower.

32 Features of SCAL indirect ACCs Cooled water recycles closely during operation, no water consumption High heat -exchange efficiency The corrosion rate of condenser can be controlled by adjusting pH in recycled water in order to prolong service cycle time of condenser Less power consumption The volume of air cooling tower is small Simple system, convenient operation and less capital construction investment

33 Unit 7 & 8 of Yangcheng Power Plant are indirect ACCs. 3 sets of powdex are used for each CPP. Powdex shows good filtration abillity for crud, but its desalination capacity is weak, so steam quality of the units didn’t reach the standard for most of running time. In order to improve the steam quality, retrofitting of CPP was carried out. 2 high-speed mixed beds were added after powdex The retrofitting has been successfully completed and put into operation in March 2009, and achieved desired results. CPP Introduction

34 Testing ItemUnitStandard Value Min.Max.Qualified Rate (%) DO in condensateμg/L3010.825.1100 Conductivity in condensateμS/cm0.30.1000.70078.0 DO in feed-waterμg/L70.124.192.7 Conductivity in feed waterμS/cm0.20.1041.81038.0 S i O 2 in feed waterμg/L203.037.894.5 Conductivity in boiler waterμS/cm1.50.1262.03099.7 S i O 2 in boiler waterμg/L20038.652097.6 Conductivity in main steamμS/cm0.20.0810.65722.5 S i O 2 in main steamμg/L202.94998.0 2007.8-2008.9 S i O 2, organism, CO 2 and other impurities in condensate couldn’t be removed after powdex. It is just depended on boiler blowdown. This is the main reason of high conductivity in steam. Steam quality of unit 8 before retrofitting

35 Testing ItemUnitStandar d Value Min.Max.Qualified Rate (%) DO in condensateμg/L3010.822.4100 Conductivity in condensateμS/cm0.30.1200.258100 DO in feed-waterμg/L72.86.8100 Conductivity in feed waterμS/cm0.20.1040.195100 S i O 2 in feed waterμg/L205.612.5100 Conductivity in boiler waterμS/cm1.50.1260.256100 S i O 2 in boiler waterμg/L20058.6125100 Conductivity in main steamμS/cm0.20.0810.159100 S i O 2 in main steamμg/L204.812.4100 2009.3 After retrofitting, conductivity in the system decreased clearly. The effluent quality of high speed mixed beds is still good after nearly 1 month operation. It achieved the desired results. Steam quality of unit 8 after retrofitting

36 Thanks for your attention !

37 Welcome to China ! Welcome to Xian ! Welcome to TPRI !

38 Wenhua Tian : 86-029-82102246 ( Office ) 86-13991302260 Email : tianwenhua@tpri.com.cn Huiyong He : 86-029-82102570 ( Office ) 86-13609111635 Email : hehuiyong@tpri.com.cn

39 Mixed Bed Cylindrical MB

40 Methods to decrease DO Strengthen the welding management and improve its quality, try to decrease the air leakage of vacuum System retrofitting----Case The condensate tank was combined to the exhaust air cooling device. After through the nozzle, the makeup water goes to the throat of exhaust device. It can lead to an increase of the secondary removal of oxygen in returned condensate. The condensate tank was combined to the exhaust air cooling device. After through the nozzle, the makeup water goes to the throat of exhaust device. It can lead to an increase of the secondary removal of oxygen in returned condensate.


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