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Distribution Lightning Protection Pilot Projects Reliability Engineering Team Lightning Arrester Initiative Presented by Tim Constanzo, PE.

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Presentation on theme: "Distribution Lightning Protection Pilot Projects Reliability Engineering Team Lightning Arrester Initiative Presented by Tim Constanzo, PE."— Presentation transcript:

1 Distribution Lightning Protection Pilot Projects Reliability Engineering Team Lightning Arrester Initiative Presented by Tim Constanzo, PE

2 Where it all started Corporate initiative to improve reliability Reliability Summit Root cause analysis methodology  Relay philosophy/settings  Maintenance, allocation of resources  Backbone initiative (distribution system design)  Lightning arresters (LA’s)

3 Problem Statement Lightning arresters (LAs) are believed to be the cause of an unacceptable frequency and duration of customer interruptions and outages.

4 Probing Questions How bad is it? Why/how are LA’s failing? How effective is current application of LA’s on system?

5 How bad is it? Estimated population: 39,000 35kV line LAs 300,000 35kV equipment LAs Total 35kV LAs: 339,000 35kV LAs issued for maintenance FYE 2005: 500 Ratio of replacements to total population: 0.15% Circuit outages in FYE 2005 LA related: 135 LA related rate of circuit outages: 8.7%

6 How/why are LA’s failing? Fishbone and Pareto graphs/Root Cause LA failure categories:  Proper isolator operation (not a failure!)  Design/Manufacturing defects  Installation Design/Practice  Thermal Runaway

7 Normal Operation Isolator designed to operate when capacity of LA is exceeded Lightning TOV No outage caused Loss of protection until replaced Reduced BIL/CFO until replaced

8 LA Design/Manufacturing Issues Poor design/manufacturing Poor seals Voids under sheds Recommendation: Revise LA standards to eliminate designs with poor seal and voids under sheds.

9 Failure due to moisture ingress

10 Installation Design Current installation design/practice Long leads wrapping around primary Reduced Insulation/BIL after isolator operates Recommendations: Shorter leads Eliminate insulating bracket

11 Tracking Failure of Bracket

12 Installation T & E Option

13 Thermal Runaway Cause: Aging zinc oxide block material Moisture ingress (most common) Effect: High leakage current Marginalized MCOV Elevated temperature Recommendations: IR patrol removal when +10°C/18°F above ambient

14 Current Application of LA’s Line arresters 27 kV/22 kV MCOV (Heavy Duty) ¼-mile spacing, all phases Equipment arresters 27 kV/22 kV MCOV (Heavy Duty) All equipment

15 Evaluating LA Application TFlash modeling cases: Baseline: no arresters Arresters @ ¼ mile, 3 phases Every pole, center phase only Every pole, raised center phase only Every pole, 3 phases

16 TFlash Results

17 Conclusions/Recommendations Discontinue current application: “¼-mile” Let attrition remove line LAs Maintain LAs protecting equipment Apply only when/where lightning is an issue Circuits requiring higher reliability High exposure Use higher voltage rated LA (27 -> 30 kV)

18 Lightning Arrestor Initiative Going Forward T&E lightning arrestor installation arrangements Static wire (no arresters) LA’s center phase only, every pole Further modeling in TFlash Evaluate costs of various arrangements

19 Questions?


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