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Managing Pressure Vessels with Known Flaws

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Presentation on theme: "Managing Pressure Vessels with Known Flaws"— Presentation transcript:

1 Managing Pressure Vessels with Known Flaws
By Augusto Roveredo, Corrosion Project Manager, Sherritt Metals , and Ana Benz, Specialty Services, IRISNDT

2 What Will Be Presented? How the Heads Were Replaced
Information on the: Intricate Design and Construction of the Vessels. Inspections Performed and their Findings. Deciding factors for choosing whether to replace the heads. How a Temper Bead Welding Procedure Was Developed Based on the National Board Inspection Code RD-1000. Head and Nozzle Replacements. Project Milestones. What Was Found Inspecting the Removed Heads

3 Leach Reactors- Background
Four trains with four reactors each have been in a very corrosive service for almost 50 years. The 212 grade B carbon steel is clad with lead lining for corrosion protection.

4 Leach Reactors- Background
The lead lining is covered by special corrosion and erosion resistant brick layers.

5 Results of NDE Inspections prior to Head Replacements
Internal inspections only allow one to observe the condition of the bricks. In 1998 and 1999, during routine clean out cycles, Trains 1 and 2 were subjected to a design code compliance and to a non-destructive evaluation. The reactor shells had insignificant wall losses and were in good condition. The reactor drain nozzle flange to cone connection had thinned areas and previous weld repairs that did not meet ASME Section VIII, Division 1 requirements.

6 Results of NDE Inspections … Cont’d
The heads had: Minute cracks on the external surface. Nozzles with extensive internal erosion/corrosion losses. Some localized eroded/corroded areas. Internal pits on the inside surface of the head, beneath manway repad covered surfaces. Large shell nozzles had cracks along the toes of welds joining the repad to the shell. The anchor bolts fixing the reactors to the ground concrete pads were corroded extensively. During these inspections, IRISNDT personnel were informed that the inside surfaces of some reactor heads had had cracks previously. Some openings did not meet the ASME Section VIII, Division 1, 1998 reinforcement requirements.

7 Based on the NDE Inspections:
Fitness for service calculations were performed to determine the remaining life of the nozzles. These indicated that the nozzles would leak instead of rupturing, i.e. “leak before break” The corrosion rates of the head nozzles were estimated by 2003 to be as high as inch per year. Attempted to assess the possible growth rate and life expectancy associated with the possible head cracks.

8 Should the Nozzles or the Complete Heads Be Replaced?
The replacement of only nozzles would not answer all the concerns identified with the head condition or the remaining life expectancy. Complete head replacement would allow for homogeneous lead lining. Nozzle replacement would be subject to installing panel leading in the overhead position.

9 Welding on the Vessels - Considerations
The welding procedure had to be optimized to decrease lead loss during welding. Other challenges were: Joining of A212 grade B carbon steel to SA 516 Grade 70 carbon steel. This entailed dealing with the A212’s coarse grain structure. Minimizing the residual stresses from welding. This encompassed trying to minimize the hardness values in the heat affected zone. Minimizing down time.

10 Welding Procedure Optimization
As well as minimizing the lead melting, a second objective was to obtain welds similar or better in quality than the originally post weld heat treated welds. This implied obtaining welds with low residual stresses that would have low hardness values and reasonable impact toughness. Several procedures were developed as per ASME Section IX. The procedures were qualified. The first procedure tested resulted in hardness values as high as 382 HV. This value was unacceptable.

11 Welding Procedure Optimization Weld Coupon C
This procedure is that described as Welding Method 3 in the National Board Inspection Code RD-1050. Preheat temperature min: 425 deg. F. Inter-pass temperature max: 450 deg. F. String or weave bead: stringer bead only. Initial and inter-pass cleaning: half bead technique first 4 passes 3/32” and 1/8” electrode, grinding and wire brush between passes. Travel speed (range): 4-8 inches per minute.

12 Welding Procedure Optimization Weld Coupon C
Macro of Weld Coupon C Very small HAZ, indicative of high cooling rates, high residual stresses and hardness values.

13 Welding Procedure Optimization Weld Coupon D
Preheat temperature min: 425 deg. F. Inter-pass temperature max: 450 deg. F. String or weave bead: stringer bead only. Initial and inter-pass cleaning: half bead technique first 4 passes 3/32” and 1/8” electrode, grinding and wire brush between passes. Travel speed (range): 4-8 inches per minute. No changes from Weld Coupon C.

14 Welding Procedure Optimization: Weld Coupon D Continued…
Changed from Weld Coupon C. Apply Butter Pass 1 along the joint edges from the root to the face of the plate. Remove half of the Butter Pass 1 by grinding. Apply Butter Pass 2. Grind cap flush and re-cap, then grind flush again.

15 Welding Procedure Optimization Macro of Weld Coupon D
Bigger HAZ, indicative of lower cooling rates. Lower hardness values.

16 Welding Procedure Optimization Comparison of Hardness Values
Weld Coupon D Weld Coupon C 226 196 254 230 234 222 260 217 238 266 248 15 177 216 219 226 251 168 257 187 226 226 226 158 x 184 269 x 165 171 210 193 212 212 171

17 Welding Procedure Optimization Conclusion
The initial welding procedure coupons had hardness values in excess of 382 HV. With the additions of a buttering pass and higher preheat the HAZ hardness values dropped to a maximum of 269 HV. The HAZ impact properties were tested at –29°F. They met the ASME SA 516 Grade 70 requirements for operation at –29°F.

18 Replacing the Heads and Nozzles – the Project Starts
Preparation for an international project. Weld repairs. Weld final inspections and approval.

19 Preparation: Where Should the Heads Be Cut?
The shell plate was inspected with ultrasound to ensure that the area to be cut was free of extensive laminations. The cutting line was chosen 18” below the head to shell seam; this would facilitate lead repairs. The vessels were strapped to size the new heads.

20 Preparation: Purchase of New Heads
Two SA516 Gr. 70, 2:1 elliptical heads and shell assemblies with homogeneous lead lining were purchased for Leach Train 1 vessels‘ B and D. The nozzle design was changed from nozzles with repads to self reinforced nozzles. The diameter of the manway nozzle was increased from 24” to 30” in order to accommodate additional 2” acid brick lining. The heads were fabricated in Canada and carry a CRN registration.

21 Preparation: Purchase of New Nozzles
Additional nozzles were purchased to replace thinned nozzles on the Leach Train 1 Vessels A and C.

22 Preparation: The Brick Lined New Heads

23 Preparation: Qualifying the Welders to the Procedure
The Canadian company contracted to weld the heads and nozzles performed welding procedure qualification and welder performance qualification tests.

24 Preparation: Showing the Welders the Importance of Their Contribution
For the reactor welds, improper welding techniques/workmanship could result in: High residual stresses. High hardness values. Areas more prone to cracking than those with lower residual stresses.

25 Showing the Welders the Importance of Their Contribution
An example was shown to the welders of a nozzle weld that failed due to high residual welding stresses (inadequate post weld heat treatment)

26 The Result of an Inadequate Post Weld Heat Treatment

27 The Result of an Inadequate Post Weld Heat Treatment

28 Execution: Project Milestones (What We Had to Achieve)
Meet all requirements of ASME section VIII, Division 1. Complete the installation of the two heads as outlined in an 11 day schedule. Complete the project within budget. Complete the project with zero loss time accidents.

29 Execution: Reactor Cut Line Being Prepared
A cut line platform was designed, fabricated and installed to ensure safety for the workers.

30 Execution: Radiograph Torch Cutting
An oxygen and acetylene radiograph torch assembly was tack welded to the existing shell section.

31 Execution: Completed Torch Cut

32 Execution: Head Being Removed

33 Execution: Lead Being Removed by Torch

34 Execution: Bevel Being Cut by Torch

35 Execution: Bevel Prep Final Product

36 Execution: New Head Being Positioned

37 Execution: Installation of Heating Coils

38 Execution: Insulation Wrap Around Heating Coils

39 Execution: Stringer Beads Being Welded on Inside Surface

40 Execution: Dry Magnetic Particle Examination of the Root Pass

41 Finished Internal Weld Finished External Weld
Execution: Finished Internal Weld Finished External Weld

42 Execution: External Weld Cap Ground Flush

43 Execution: Lead Panel of the New Joint
Lead panel joints were inspected with liquid penetrant.

44 Execution: Nozzle Butter Pass
Integral nozzles were manufactured. Welding trials were performed on the removed heads.

45 Execution: Preparing the Head Surface where the New Nozzle Was to Be Inserted
The prepared base metal bevelled surfaces were subjected to black on white magnetic particle inspections.

46 Execution: Replacement Nozzle Fit-up

47 Execution: Nozzle Completed Outside Weld

48 Execution: Nozzle Completed Inside Weld

49 Weld Final Inspections and Approval: ASME Compliance
A North American Authorized Pressure Vessel Fabrication Inspector performed all the checks that would have been required in North America for an equivalent repair and modification.

50 Weld Final Inspections and Approval:
Radiography of the New Weld In Situ Metallography and Hardness Tests

51 Execution: Final Steps
Bricks were replaced in the closing seam area. Hydrostatic testing was not required since the repair weld was radiographed. Nevertheless, the vessels were hydrostatically tested. A new deck was installed. The temporary work platform was removed.

52 Project Milestones: Conclusion
Meet all requirements of ASME section VIII, Division 1…..Accomplished. Complete the installation of the two heads as outlined in the 11 day schedule….Completed one day under schedule. Complete the project within budget…. Came in under budget. Complete the project with zero loss time accidents…. Completed without a loss time accident.

53 Project Completed? – What Was Found Inspecting the Removed Heads
The Head D manhole and several of its nozzles were cut. Their cross-sections were examined and several deficiencies were found: extensive thickness losses large cracks that followed the deposited weld metal fusion line the cracks appeared to have grown after fabrication small cracks on the manway nozzle

54 Tasks Once the Cracks Were Identified
Fully characterize and identify main cracks and other deficiencies. Determine fracture mode. Perform finite element and fitness for service evaluations to determine the major stresses that contributed to the failure. Determine remaining life. Develop repair and replacement plans.

55 Extensive Nozzle Thickness Losses
The nozzles of removed heads had extensive thickness losses, as expected.

56 Head Manhole to Head Joint Had Large Cracks
The head manhole to head joint had large cracks that followed the deposited weld metal fusion line between the deposited weld metal and the head. C R AC K S

57 Morphology of Head Manhole to Head Joint Cracks
The cracks appeared to have grown after fabrication since multiple fracture morphologies were apparent: Some fracture surfaces had transgranular cleavage cracks indicative of a linear elastic fracture. Other fracture surfaces had welding related slag remnants Some fracture surfaces had dimples indicative of a plastic overload.

58 Fracture Surfaces Were Covered with Heavy Non-Metallic Layers
Welding related slag remnants on fractures

59 The Welds Had Relatively Low Hardness Values
Often, welding related fractures with cleavage cracks can be the result of hydrogen embrittlement. However, these cracks typically develop in the heat affected zone in metal of hardness values significantly greater than those measured here.

60 What Caused the Cracks? Finite Element and Fitness for Service Analyses
The cracks are subsurface and consequently are subjected to relatively low stress intensity values. The thermal and mechanical stresses were evaluated for the following conditions: While the vessels are in-service During hydrostatic tests. During the most severe start-up and shutdown conditions.

61 Thermal and Mechanical Stresses
These analyses found that the most severe stress conditions for the weld crack occur during hydrostatic tests at 1.3 times the service pressure. The most severe start-up and shutdown conditions resulted in thermal stresses that were either compressive or significantly smaller than the hydrostatic test stresses.

62 Thermal and Mechanical Stresses … Cont’d
Even the hydrostatic stresses in the nozzle to head weld were relatively low; this suggested the following possibilities: The residual welding stresses subsequent to post weld heat treatment were significant. Previously, they were considered insignificant since the weld had been stress relieved. This section of the head is subjected to an unknown but significant source of stress.

63 Thermal and Mechanical Stresses … Cont’d
The residual welding stresses subsequent to post weld heat treatment were assessed. Considered the possibility that this section of the head is subjected to an unknown but significant source of stress.

64 Stress Intensity Factor, Residual Stress Only

65 Stress Intensity Factor, Residual Stress + 700psi
For a 700 psi hydrostatic stress and Method 1 residual stresses, the stress intensity (the crack driving force) is greater than 30 ksiin for 0.3WT to 0.7WT deep cracks. For cracks deeper than 0.7WT, the stress intensity drops below 30 ksiin.

66 Stress Intensity Factor, Residual Stress + 700psi
Assuming that the fracture toughness of the HAZ is 30 ksiin, this predicts that brittle cracks can reach a 0.7WT depth and then arrest. This is consistent with the crack depths observed to date.

67 Stress Intensity Factor, Residual Stress + 900psi
For a 900 psi hydrostatic stress and Method 1 residual stresses, the stress intensity is greater than 30 ksiin for 0.2WT to 0.8WT deep cracks. For cracks deeper than 0.8WT, the stress intensity drops below 30 ksiin. This predicts that brittle cracks can reach a depth of 0.8WT and then arrest.

68 Why a Fracture Toughness of 30 Ksiin?
A 198 ksiin was assessed after measuring the J Fracture Toughness for the head parent material. However, this value was not used for the critical crack length assessments since: It was measured for the head parent material. The head parent material is tougher than the fusion zone where the crack grew. The cleavage fractures noted are not consistent with a 198 ksiin toughness.

69 Why a fracture toughness of 30 ksiin?… Cont’d
Temperature versus Energy Absorption Location 212F Ft-Lbs. 122F 70F -29F Weld Average - 115 64 Head Average 53 37 23 7

70 The Remaining Life Cannot Be Assessed
The material ahead of the crack could consist mainly of slag and/or non-fusion (as noted in some sections examined). This material would have negligible toughness in which case the weld would fracture through thickness. The fillet weld joining the repad to the manway could maintain the parts from separating from the vessel. However, this weld also has cracks, non-fusion and slag. The reactors may have been subjected to stresses greater than those considered here. The cracks will likely continue growing and linking around the circumference. The stress intensity values for the cracks to link around the manhole circumference are greater than those for the crack to propagate through the thickness.

71 What Next? Continue the manhole to head joint crack sizing inspections
Continue the hydrostatic tests prior to start-up. If the manway to head weld fails, it would likely fail during the hydrostatic test.  Prioritize which heads should be replaced assessing which are the deeper cracks.


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